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我投入了大量的时间来创建一个DFB程序,用于执行输入流的预处理。因为默认的DFB模拟器(V1.4)是无用的,所以这个代码的开发需要将PSoC造器版本4.1降低到2.2,因为它是能够运行Chris Keeser的扩展模拟器的最后版本,它至少显示了一些东西。CyPress支持也没有使我的任务更容易:所有四个我最近的bug报告都被标记为“取消”,尽管附加的片段显示直接违反DFB规范。他们回答了他们默认的“走开”的信息,那是他们告诉我的。
去社区论坛,好像社区成员可以访问模拟器源,或者可以调整误导/惊人错误的文档。我不知道这种敌意的原因,但如果它想驱逐顾客,那肯定是一种魅力。 但是要点是:附加的项目有“DSP”页面,它包含一个DFB实例和TS程序。它由两个DMA通道馈送,结果由另两个DMA收集。确切的输入值是无关的,问题是在控制流级别,而不是用错误的计算结果。所有四个DMA通道工作正常,用几个阶段-Gt;保持转发片段检查。C是这样做的:配置测试环境,让我看到作用域上的调试信号。该代码在两个模拟器(即DFB汇编程序1.4和Keeser的)上进行了良好的仿真,得到的结果与C++参考实现完全一致。在一个真正的芯片上,它是一场史诗般的灾难。DFB程序由两个独立的计算引擎组成,但最终它们都归结为相同的任务:计算3个第四阶CIC滤波器的序列,每一个都抽取4。因此组合抽取系数为64。为了将硬度降低至少一半,我绕过了“监视”部分,但是即使是更简单的SDR部分也被打破了。正确的正确标志是输出DMA传输的频率:对于每秒310000个输入采样,输出应该是64倍更少,即每秒4843.75个采样。范围为40 .50kHz,没有明显的图案。尽管它的名称,DFB ALU缺乏任何逻辑指令,所以组合的“64”计数器被实现为以复杂的增量/补偿器方式更新的3个2位计数器的压缩阵列。我重新使用了一个信号量来检查CSBJCICSKBBY集成状态访问的频率。太频繁了。所需的场景如下:每秒输入CSAYSDRYPROCEDATA数据310E3次,然后在每个I/Q路径上每第四个周期集成CSBJCICSCOMBY,在每个8个输入样本之后转换为两个后续访问,因为每个路径都有专用的CIC滤波器。然后进一步前进,在每一个已过滤的第四个周期中的每第四个周期中移动到更高的CIC电平,即每16个周期一次,然后每64个周期一次,然后将结果存储在HOLDB中。它是这样设计的,这就是模拟器上发生的事情。 这次我想找出柏柏尔工具到底出了什么毛病,但没劲了。我正把整个PSoC冒险扔到垃圾箱,切换到更好的指定Xilinx ZYNQ家族,但我后悔所有花了的时间和金钱,所以请你看看附件中的项目并尝试猜测DFB的物理实现在哪里发散。它的规格如此惊人,以至于我的代码变得毫无用处? CyWrk.CaseV01.Zip 1.2兆字节 以上来自于百度翻译 以下为原文 I have invested considerable amount of time in creating a DFB program intended to perform input streams' preprocessing. Because the default DFB simulator (v1.4) is next to useless, the development of this code required downgrade of PSocCreator version 4.1 to 2.2, because it is the last version that is able to run Chris Keeser's extended simulator, which at least shows you something. Cypress support didn't make my task easier either: all four of my recent bug reports have been marked as "Cancelled", despite the attached snippets which show direct violation of the DFB specification. They replied with their default "go away" message, that is they told me to go to the community forum, as if the community members had access to the simulator sources or could adjust the misleading/strikingly wrong documentation. I don't know the reason for this hostility, but if its intended to repel customers, it surely works like a chARM. But to the point: the attached project has the "DSP" page, which contains a DFB instance together with ts program. It is fed by two DMA channels and the results are collected by another two. The exact input values are irrelevant, the problem is at the control flow level, not with incorrectly computed results. All four DMA channels work correctly, checked that with a few stage->hold forwarding snippets. This is all what main.c does: configure the testing environment and lets me see the debug signals on the scope. The code simulates well on both simulators (i.e. the DFB assembler 1.4's and Keeser's) and the obtained results are in full agreement with the C++ reference implementation. On a real chip it is an epic disaster. The DFB program is composed of two independent calculation engines, but finally they all boil down to the same task: compute a sequence of 3 4th order CIC filters, each decimating by 4. So the combined decimation factor is exactly 64. To cut the hardness by at least a half, I bypassed the 'monitoring' part, but even the much simpler SDR part is broken. The obvious sign of correctness would be the the frequency of the output DMA transfers: for 310,000 input samples per second the output should be 64 times less, i.e. 4843.75 samples per second. The scope shows 40..50kHz with no obvious pattern. Despite its name, the DFB ALU lacks any logical instructions, so the combined "to 64" counter is implemented as a packed array of 3 2-bit counters updated in a complex delta/compensator way. I've reused one of the semaphores to check how often the c***_cic_comb_integrate state is visited. Far too often. The desired scenario is as follows: enter csa_sdr_process_data 310e3 times per second, then go to c***_cic_comb_integrate every fourth cycle on each of the I/Q paths, which translates into two subsequent visits after each 8 input samples, because each path has a dedicated CIC filter. And then go further and move to the higher CIC level after every fourth of the already filtered fourth cycles, i.e. once per 16 cycles, then once per 64, then store the result in holdb. It was designed this way and this is what happens on the simulator. I was trying to figure out what is going wrong this time with the Cypress tools, but ran out of steam. I'm at the verge of throwing the entire PSOC adventure to the dustbin and switching to the much better specified XIlinx Zynq family, but I regret all the spent time and money, so could you please have a look at the attached project and try to guess where the physical implementation of DFB diverges with its specification so strikingly that my code becomes useless?
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很抱歉听到你的麻烦。我下载了你的项目并看了看,尽管这看起来很先进,可能超出了我的理解,但我确实尝试过了。现在看来这是一个愚蠢的建议,但有一件事是可能的。我有一个项目,如果我启用了“停止XTAL启动错误”,我的项目将无法工作。似乎值得一试,因为它只在一个盒子里滴答作响。
希望你能找出答案。 以上来自于百度翻译 以下为原文 Sorry to hear your having troubles with this. I downloaded your project and had a look, and even though this looks to me like quite advanced and probably beyond my understanding i did try and work my way through it. Now this may seem as a stupid suggestion but one thing stood out as a possible querk. I had a project where if i enabled the 'Halt on XTAL startup error' my project would not work. Seems worth a try as its only a tick in a box. Hope you figure it out. |
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xtl1117 发表于 2018-12-25 06:52 谢谢你的输入。你是正确的,这个项目有几个小问题,但它只是意味着接受工作的“器官”从一个较早的,死的项目已经失败,并因此表明,如果有一种方式在PSoC5LP上做,它引导通过DFB协处理器。主臂芯刚好不够实时。这是正确的方法,如果我可以这么说,因为我浪费了“仅仅”一个月来发展DFB程序,没有大惊喜等待我直到最后。 我之前有“停止XTAL启动错误”的完全相同的问题,但这里并不是问题。如果DFB不能按照文档和模拟器去做/已经做的话,就根本没有必要继续PSOC家族,并且切换到符合其自身规范的东西,实际上是由一个称职的工程师团队支持的。如果你允许像巴德朗或Keeser这样的人离开,你的结果就来了。 塞浦路斯很乐意为这个问题指派一个应用工程师,但坦率地说,我并不期待成功。我刚给他们发送了四个简化的DFB程序,这些程序应该简单地将通道B输入转发到输出(减去一个不重要的常数之间,但是我们讨论的是完全错误的控制流模式,而不是关于正确路径路径上的错误结果)。 他们都工作错误,但通过插入越来越多的NOP [即,ACU(保持,保持)DMUX(SA,SA)ALU(保持)MAC(保持)]输出通道DMA DRQ频率,连接到HOLDB…上升。让他们先解释一下。但是当你问模拟器…Mharharhar:-D这个软件是如此不堪一击…下载VIVADO。 以上来自于百度翻译 以下为原文 Thank you for your input. You're right that there are several minor issues with this project, but it is just meant to accept working "organs" from an earlier, dead project which has already failed and hence shown that if there is a way to do it on PSOC5LP at all, it leads through the DFB coprocessor. The main ARM core would just not be real-time enough. This turned out to be the correct approach, if I may say so, because I've wasted "just" a month to develop the DFB program first, no big surprise waiting for me till the very end. I had exactly the same issue with 'Halt on XTAL startup error' earlier, but it's not a problem here (yet). If DFB cannot do what it should be able to do/already does according to the documentation and the simulator, there is no point in continuing with the PSOC family at all and switch ASAP to something that conforms to its own specification and actually is supported by a competent crew of engineers. If you allow the people like Budlong or Keeser to leave, here come your results. Cypress was kind enough to assign an Application Engineer to this issue, but, frankly, I don't expect much success. I've just sent them four more simplified DFB programs, which should simply forward the channel B input to the output (subtracting an unimportant constant in between, but we're talking about totally wrong control flow patterns, not about the luxurious wrong results on the correct paths case...). They all work wrong, but by inserting more and more nops [that is, acu(hold, hold) dmux(sa, sa) alu(hold) mac(hold)] the output channel DMA DRQ frequency, tied to holdB... rises. Let them first explain this. But when you ask the simulator... Mharharhar :-D This software is so unbelievalby broken... Downloading Vivado. |
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